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750 kV官东Ⅰ线地线滑移原因分析及处理

Analysis and Disposal of 750 kV Guan-Dong Ⅰ Transmission Line Ground Wires Slip
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摘要 在超高压输电线路地形高差较大且连续倾斜的档,地线在运行中受温度、微气象、风害、覆冰等外界环境影响常发生滑移的情况.以750 kV官东Ⅰ线为例,分析了地线滑移的主要原因是高差较大的连续倾斜档受力不平衡.提出了简单经济、切实可行的技改方案:地形起伏较大的塔位普通悬垂串改造为悬垂开断形式,改善了地线、线夹以及金具的受力,充分发挥了金具的灵活性和自身调节裕度,有效缓冲了外界环境影响产生的不平衡张力. In the extra high voltage line span which is inclined and in complex landform condition,the ground wires often slip affected by temperature,microclimate,wind,ice and other outside environment.According to 750 kV Guan-Dong I Transmission Line for example,this paper analyzes the main reason of the ground line slip in the situation described above with the conclusion of unbalance force,and suggests a simple,economical and practical method,which changes the common pendency string to the type of pendency-breaking on the tower with biggish hypsography,improves ground line,line clips,and gold tool's force bear,highly exertes the gold tool's agility and self-regulate tolerance degree,effectively buffers the imbalance tension influenced by the outside environment.
作者 马军 MA Jun 
机构地区 [
出处 《电网与水力发电进展》 2007年第9期62-65,共4页
关键词 750KV线路 地线滑移 普通悬垂串 悬垂开断 750 kV transmission line ground wires slip common pendency string pendency-breaking
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参考文献3

  • 1[1]刘振亚.国家电网公司750 kV输变电示范工程建设总结(科研分册)[M].北京:中国电力出版社,2006.
  • 2[3]Q/GDW 115-2004,750 kV架空送电线路施工及验收规范[S].
  • 3[4]SDJ226-1987,架空送电线路导线及避雷线液压施工工艺规程(试行)[S].北京:水利电力出版社,1987.

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