摘要
经对星 119井的压前、二次压裂后测试资料的试井分析 ,评价了高能气体压裂和二氧化碳酸冻胶压裂措施效果 ,确定了压后低产原因是由于储层渗透性差 ,不是油藏改造工艺问题 ,从而为该区的下一步勘探和开发提供科学依据。
By analyzing for pre-fracture and the second post fracture testing data of Xing119 well, the treatment effect of high power gas fracture and fracture with CO2 acid gel have been evaluated to determine that the reason of causing low production after be fractured is for poor percolation, not for treatment technology which provide a scientific basis for the next step of exploration and development. By analysis of testing results, it is illustrated that testing data is one of the effective methods to evaluate fracture effect at present.
出处
《油气井测试》
EI
2004年第5期22-23,共2页
Well Testing