摘要
针对协调控制系统的非线性、耦合、燃料大惯性特性,首先建立协调控制系统非线性模型,然后对此模型在3个工况点下进行线性化,设计了与之对应的多变量动态解耦PID控制器,并进行了现场投运。实际调试结果证明了这种新型协调控制系统设计的有效性。
According to the characteristics of the coordinated control system, a nonlinear model of the system is proposed. The model is linearized under three work conditions. The multi-variable dynamic decoupling PID controller is designed. The field application shows its validity.
出处
《华北电力大学学报(自然科学版)》
CAS
北大核心
2005年第5期75-78,共4页
Journal of North China Electric Power University:Natural Science Edition
关键词
动态解耦
多变量控制
协调控制系统
dynamic decoupling
multi-variable control
coordinated control system