摘要
对秦京管道因混输冀东原油后秦皇岛-迁安管段输量下降16%,造成输油设备与运行工况不相匹配,出现节流损失大、能源浪费大的问题进行了分析。通过采取相应的技术改造措施,制定了秦京管道混输后的近期和长期优化运行方案。该方案实施效果表明,优化运行方案科学合理,目的性明确,管道运行安全经济。
The analysis on the mismatch between transportation equipments and operation condition, more throttling loss and power consumption in Qinhuangdao-Beijing Oil Pipeline is made. This problem comes from the Jidong Crude's blended transportation in this pipeline which results in 16% decrease in oil throughput in Qinhuangdao-Qian'an pipeline section. In allusion to this problem,the corresponding technical measures for short-term and long-term optimized operation programs are worked out.
出处
《油气储运》
CAS
北大核心
2006年第3期17-22,共6页
Oil & Gas Storage and Transportation
关键词
输油管道
技术改造
优化运行
分析
oil pipeline,technical reform,optimizing operation,analysis