期刊文献+

气举作业中连续油管腐蚀断裂原因 被引量:9

Corrosion Cracking Cause of Coiled Tubing in Gas Lift Operation
下载PDF
导出
摘要 某海上气井连续氮气气举作业61.5h后,发生连续油管断裂,观察发现连续油管外壁腐蚀严重。通过宏观和微观分析、理化性能检验、X射线衍射和模拟试验,对腐蚀油管进行了失效分析。结果表明,气举作业所用氮气携带的O_2和井内CO_2共同作用造成了连续油管腐蚀破坏,氧腐蚀是造成短时间内连续油管严重腐蚀的主要因素。针对此结论和现场工况,采取除氧防腐蚀措施,解决了现场作业中连续油管的腐蚀问题。 A coiled tubing in an offshore gas well cracked and suffered serious corrosion after nitrogen gas-lift operation for 61.5 h. The failure cause of the tubing was studied by macro and micro analysis, physical and chemical properties testing, X-ray energy spectrum analysis and stimulated corrosion test. The results showed that the combined effect of O2 carried by N2 and CO2 in the wet gas well corroded the coiled tubing. The O2 corrosion was the main reason of the corrosion of coiled tubing in short time. According to the results and the on-site conditions, measures to remove O2 was taken and the corrosion problem was resolved.
出处 《腐蚀与防护》 CAS 北大核心 2011年第9期758-760,共3页 Corrosion & Protection
关键词 氮气气举 连续油管 氧腐蚀 二氧化碳腐蚀 nitrogen gas-lift coiled tubing O2 corrosion CO2 corrosion
  • 相关文献

同被引文献100

引证文献9

二级引证文献24

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部