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大化水电站二期导流工程导流明渠泥沙运动与冲淤 被引量:1

^Sediment Sluicing& Sediment Motion for Construction Diversion of Second Stage on the Dahua Hydropower Station
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摘要 大化水电站二期导流工程截流前,导流明渠基本堵塞,靠人力及机械清淤无法按时实现截流。经过分析研究,采用主河槽预抛方案提高上游水位,使导流明渠水流速由1.0m/s逐渐增大到3.25m/s,在17天内冲走25.2万m3淤积泥砂,实现了按计划截流。 The amount of sediment in the diversion channel of Dahua hydropower station reached 252 000 m3 which almost blocked up the channel before the second stage of river-damming of diversion construction. Clearing away the sediment by manpower and machine could not realize the riverdamming in a planned way. The employ of throw stones in advance to main river led scheme raisedthe water level of upper reaches and increased the waterflow velocity of diversion channel from1. 0 m/s to 3. 25 m/s, which resulted in the sluicing away of 252 000 m3 sediment within 17 days.Thus damming the river was achieved in a planned way.
作者 王涛
机构地区 广西水电工程局
出处 《广西科学》 CAS 1995年第2期67-73,共7页 Guangxi Sciences
关键词 大化水电站 起动流速 导流明渠 泥沙运动 冲淤 Dahua hydropower station incipient velocity diversion channel sediment motion sluicing sediment.
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