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厌氧/二级AO+高效沉淀/反硝化深床滤池工艺用于污水厂准Ⅳ类提标扩建 被引量:3

Anaerobic/Secondary AO Together with High-Efficiency Precipitation/Denitrification Deep Bed Filter Process used for Upgradation and Reconstruction Project of Quasi-Ⅳ Standards in Wastewater treatment plant
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摘要 温岭市某污水处理厂一期工程设计规模0.5×104 m3/d,生物处理采用SBR工艺,出水执行《城镇污水处理厂污染物排放标准》(GB18918-2002)一级B标准。本期工程包括改建、扩建两部分,改建工程规模为0.5×104 m3/d,将原SBR池改建为二级AO池,扩建工程规模为0.5×104 m3/d,采用厌氧/二级AO工艺,并新建1.0×104 m3/d深度处理段(采用高效沉淀池、反硝化深床滤池工艺)。此次提标扩建后总处理规模达到1.0×104 m3/d,出水达到准地表Ⅳ类排放标准。 The design scale of the first phase of a wastewater treatment plant in Wenling City is 0.5×10^4 m^3/d, and SBR is used for biological treatment. The effluent quality was required to met the first level B criteria in the Discharge Standard of Pollutants for Municipal Wastewater Treatment Plant(GB 18918-2002).Upgradation and Reconstruction are the main two parts of this project. The scale of the reconstruction project is 0.5×10^4 m^3/d, and convert SBR pool into a secondary AO pool. While the next reconstruction project scale is 0.5×10^4 m^3/d., used with anaerobic/secondary AO technology. And new 1.0×10^4 m^3/d advanced treatment section is built by using High-efficiency Precipitation Tank and Denitrification Deep Bed Filter Process. After this subproject, the total treatment scale will reach 1.0×10^4 m^3/d, and the effluent quality will meet the Quasi-Ⅳ Standards.
作者 乐华斌 赖辉辉 Yue Huabin;Lai Huihui(China Gezhouba Group Investment Holdings Co.,Ltd., Wuhan 430000, Chin)
出处 《广东化工》 CAS 2018年第11期211-212,225,共3页 Guangdong Chemical Industry
关键词 提标扩建 二级AO 高效沉淀池 反硝化滤池 准地表IV类 upgradation and reconstruction secondary AO high-efficiency precipitation tank denitrification deep bed filter process quasi-IV STANDARDS
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