期刊文献+

蒲石河电站下库大坝扬压力超限原因分析 被引量:1

Analysis on excessive uplift pressure of Pushihe lower reservoir dam
下载PDF
导出
摘要 蒲石河抽水蓄能电站下库坝岸坡坝段、河床坝段部分扬压力测孔渗压系数超过设计标准。对此,综合分析了下库坝坝址区地质构造、两岸绕坝渗流及目前渗压系数计算方法。结果表明,两岸地下水高于下游水位和基岩接缝高程及基岩裂隙是导致大坝渗压系数超标的主要原因。 The seepage pressure coefficients at the bank block and the riverbed block of Pushihe lower reservoir dam exceed design standard.Therefore,this paper comprehensively analyzes the geological structure of site area,bypass seepage on both sides of the dam and current calculation method of seep?age pressure coefficient.The analysis results show that the main reasons for excessive seepage coeffi?cient include:(1)the underground water level on both sides is higher than the downstream water level and the elevation of joints in bedrock and(2)there are cracks in bedrock.
作者 张凤芹 王千 ZHANG Fengqin;WANG Qian(Fengman Hydropower Plant;不详)
出处 《大坝与安全》 2020年第1期42-44,共3页 Dam & Safety
关键词 渗压系数 地质构造 绕坝渗流 计算方式 seepage pressure coefficient geological structure bypass seepage calculation method
  • 相关文献

参考文献1

二级参考文献1

共引文献3

同被引文献6

引证文献1

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部