期刊文献+

软土地下深基坑减压降水成槽技术研究

Research on Decompression and Dewatering Trenching Technology for Underground Deep Foundation Pits in Soft Soil
下载PDF
导出
摘要 为了提升轨道交通车站深基坑工程的成槽质量和槽壁稳定性,解决整个地下工程质量安全产生问题,文章以某轨道交通3号线车站深基坑工程为研究对象,采用地下深基坑减压降水成槽技术,并通过常规成槽试验和优化后的5 m降深优化试验,对结果进行对比分析。结果表明,较小井间距条件下的减压降水显著提高了成槽质量和槽壁稳定性。优化后的方案在经济成本上也优于其他方案,能获得较为良好的施工效果,具有一定的应用价值。 In order to improve the trenching quality and trench wall stability of deep foundation pit engineering at rail transit station and solve the quality and safety problems of the entire underground engineering,this paper takes the deep foundation pit engineering at a station on rail transit line 3 as the research object,adopts the underground deep foundation pit decompression and dewatering trenching technology,and compares and analyzes the results of the conventional trenching test and the optimized 5 m depth reduction optimization test.The results show that the decompression and dewatering under the condition of smaller well spacing significantly improves the trenching quality and trench wall stability.The optimized scheme is also superior to other schemes in terms of economic cost,which can obtain better construction effect and has certain application value.
作者 胡新达 董建宁 陈高升 HU Xinda;DONG Jianning;CHEN Gaosheng(Guangcheng Construction Group Co.,Ltd.,Wenzhou 325000,Zhejiang,China)
出处 《工程技术研究》 2023年第8期41-44,共4页 Engineering and Technological Research
关键词 软土 地下工程 深基坑 降水 成槽 轨道交通车站 soft soil underground engineering deep foundation dewatering forming slot rail transit station
  • 相关文献

参考文献3

二级参考文献21

共引文献9

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部