During the production of Ti-bearing Al-killed ultra-low-carbon(ULC) steel, two different heating processes were used when the converter tapping temperature or the molten steel temperature in the Ruhrstahl–Heraeus(RH)...During the production of Ti-bearing Al-killed ultra-low-carbon(ULC) steel, two different heating processes were used when the converter tapping temperature or the molten steel temperature in the Ruhrstahl–Heraeus(RH) process was low: heating by Al addition during the RH decarburization process and final deoxidation at the end of the RH decarburization process(process-Ⅰ), and increasing the oxygen content at the end of RH decarburization, heating and final deoxidation by one-time Al addition(process-Ⅱ). Temperature increases of 10°C by different processes were studied; the results showed that the two heating processes could achieve the same heating effect. The T.[O] content in the slab and the refining process was better controlled by process-Ⅰ than by process-Ⅱ. Statistical analysis of inclusions showed that the numbers of inclusions in the slab obtained by process-Ⅰ were substantially less than those in the slab obtained by process-Ⅱ. For process-Ⅰ, the Al_2O_3 inclusions produced by Al added to induce heating were substantially removed at the end of decarburization. The amounts of inclusions were substantially greater for process-Ⅱ than for process-Ⅰ at different refining stages because of the higher dissolved oxygen concentration in process-Ⅱ. Industrial test results showed that process-Ⅰ was more beneficial for improving the cleanliness of molten steel.展开更多
For ultra-low-carbon(ULC)steel production,the higher oxygen content before Ruhrstahl-Heraeus(RH)decarburization(de-C)treatment could shorten the de-C time in the RH degasser.However,this would lead to oxidation rates ...For ultra-low-carbon(ULC)steel production,the higher oxygen content before Ruhrstahl-Heraeus(RH)decarburization(de-C)treatment could shorten the de-C time in the RH degasser.However,this would lead to oxidation rates being exceeded by molten steel production,affecting ULC steel surface quality.In this work,a carbon powder addition(CPA)process was proposed to reduce the dissolved oxygen content at the end of RH de-C through addition of carbon powder to molten steel in the vacuum vessel.Carbon and oxygen behavior during the CPA and conventional process was then studied.The results demonstrated that the de-C rate with CPA was lower compared to the conventional process,but the carbon content at the end of de-C presented no difference.The de-C reaction for CPA process took place in the four reaction sites:(1)within the bulk steel where the spontaneous CO bubbles form;(2)splashing area on the liquid steel surface;(3)Ar bubble surface;(4)molten steel surface.The CPA process could significantly reduce the dissolved oxygen content at the end of de-C,the sum content of FeO and MnO in the slag,the aluminum consumption,and the defect rate of rolled products.This was beneficial in improving ULC steel cleanliness.展开更多
基金financially supported by the National Natural Science Foundation of China (No.51404022)
文摘During the production of Ti-bearing Al-killed ultra-low-carbon(ULC) steel, two different heating processes were used when the converter tapping temperature or the molten steel temperature in the Ruhrstahl–Heraeus(RH) process was low: heating by Al addition during the RH decarburization process and final deoxidation at the end of the RH decarburization process(process-Ⅰ), and increasing the oxygen content at the end of RH decarburization, heating and final deoxidation by one-time Al addition(process-Ⅱ). Temperature increases of 10°C by different processes were studied; the results showed that the two heating processes could achieve the same heating effect. The T.[O] content in the slab and the refining process was better controlled by process-Ⅰ than by process-Ⅱ. Statistical analysis of inclusions showed that the numbers of inclusions in the slab obtained by process-Ⅰ were substantially less than those in the slab obtained by process-Ⅱ. For process-Ⅰ, the Al_2O_3 inclusions produced by Al added to induce heating were substantially removed at the end of decarburization. The amounts of inclusions were substantially greater for process-Ⅱ than for process-Ⅰ at different refining stages because of the higher dissolved oxygen concentration in process-Ⅱ. Industrial test results showed that process-Ⅰ was more beneficial for improving the cleanliness of molten steel.
基金financially supported by the National Natural Science Foundation of China(No.51874021)Fundamental Research Funds for the Central Universities of China(No.FRF-IC-18-002)State Key Laboratory of Advanced Metallurgy Foundation of China(No.41618019)
文摘For ultra-low-carbon(ULC)steel production,the higher oxygen content before Ruhrstahl-Heraeus(RH)decarburization(de-C)treatment could shorten the de-C time in the RH degasser.However,this would lead to oxidation rates being exceeded by molten steel production,affecting ULC steel surface quality.In this work,a carbon powder addition(CPA)process was proposed to reduce the dissolved oxygen content at the end of RH de-C through addition of carbon powder to molten steel in the vacuum vessel.Carbon and oxygen behavior during the CPA and conventional process was then studied.The results demonstrated that the de-C rate with CPA was lower compared to the conventional process,but the carbon content at the end of de-C presented no difference.The de-C reaction for CPA process took place in the four reaction sites:(1)within the bulk steel where the spontaneous CO bubbles form;(2)splashing area on the liquid steel surface;(3)Ar bubble surface;(4)molten steel surface.The CPA process could significantly reduce the dissolved oxygen content at the end of de-C,the sum content of FeO and MnO in the slag,the aluminum consumption,and the defect rate of rolled products.This was beneficial in improving ULC steel cleanliness.