The simulated process model of the HAc dehydration process under actual overloaded condition was conducted by amending the model of standard condition in our previous work using the process data collected from actual ...The simulated process model of the HAc dehydration process under actual overloaded condition was conducted by amending the model of standard condition in our previous work using the process data collected from actual production. Based on the actual process model, the operation optimization analysis of each plant(HAc dehydration column, decanter and NPA recycle column) was conducted using Residue Curve Maps(RCMs),sensitivity analysis and software optimization module. Based on the optimized parameters, the influence of feed impurity MA and the temperature of decanter on the separating effect and energy consumption of the whole process were analyzed. Then the whole process operation optimizing strategy was proposed with the objective that the total reboiler duty Q Total of C-1 and C-3 reaches the minimum value, keeping C-1 and C-3 at their optimized separation parameters obtained above, connecting all the broken recycle and connection streams, and using the temperature of D-1 as operation variable. The optimization result shows that the total reboiler duty Q Total of the whole process can reach the minimum value of 128.32 × 10~6 k J·h^(-1) when the temperature of decanter is 352.35 K, and it can save 5.94 × 10~6 k J·h^(-1), about 2.56 t·h^(-1) low-pressure saturated vapor.展开更多
At present, methanol to propylene(MTP) technology developed by Lurgi Company is adopted for commercial plants and refined methanol with the purity ≥99.85 wt% is required as the feed of MTP unit in Lurgi's technol...At present, methanol to propylene(MTP) technology developed by Lurgi Company is adopted for commercial plants and refined methanol with the purity ≥99.85 wt% is required as the feed of MTP unit in Lurgi's technology.Therefore, high energy cost for refined methanol production is one of the bottlenecks to improve the economy of MTP technology. Reducing the grade of feed refined methanol may be an effective method to save energy and reduce operation costs in MTP process. In this work, experiments and process simulation were carried out to investigate the influence and feasibility of degrading the methanol feed. Experiments were conducted to investigate the influence of crude methanol feed on conversion and selectivity of MTP reaction as well as the performance of ZSM-5 catalyst. The experimental results showed that degrading the methanol feed had no obvious influence on the conversion and selectivity of MTP reactions and the catalyst deactivation was caused by the carbon accumulation and metals deposition on the active sites. The process simulation results showed that the influence on the conversion and selectivity as well as the stream load of MTP process was negligible if 98 mol% methanol was used as feed. Finally, industrial experiments were conducted by adjusting the operation parameters to degrade of feed methanol of the commercial 500 kt·a^(-1) MTP unit of Ningmei Group in China. The results of industrial application illustrated that annually 180 kt fuel coal and 150 kt desalted water as well as 1770 MW·h^(-1) electricity would be saved when the water content increased from 0.01% to 0.4%. This work has identified the feasibility to improve MTP technology by degrading the methanol feed.展开更多
基金Supported by Shanghai University Youth Teacher Training Program(ZZsl15002)Shanghai Sailing Program(17YF1413100 and 17YF1428300)
文摘The simulated process model of the HAc dehydration process under actual overloaded condition was conducted by amending the model of standard condition in our previous work using the process data collected from actual production. Based on the actual process model, the operation optimization analysis of each plant(HAc dehydration column, decanter and NPA recycle column) was conducted using Residue Curve Maps(RCMs),sensitivity analysis and software optimization module. Based on the optimized parameters, the influence of feed impurity MA and the temperature of decanter on the separating effect and energy consumption of the whole process were analyzed. Then the whole process operation optimizing strategy was proposed with the objective that the total reboiler duty Q Total of C-1 and C-3 reaches the minimum value, keeping C-1 and C-3 at their optimized separation parameters obtained above, connecting all the broken recycle and connection streams, and using the temperature of D-1 as operation variable. The optimization result shows that the total reboiler duty Q Total of the whole process can reach the minimum value of 128.32 × 10~6 k J·h^(-1) when the temperature of decanter is 352.35 K, and it can save 5.94 × 10~6 k J·h^(-1), about 2.56 t·h^(-1) low-pressure saturated vapor.
基金Supported by the National Key R&D Program of China(2017YFB0601902)
文摘At present, methanol to propylene(MTP) technology developed by Lurgi Company is adopted for commercial plants and refined methanol with the purity ≥99.85 wt% is required as the feed of MTP unit in Lurgi's technology.Therefore, high energy cost for refined methanol production is one of the bottlenecks to improve the economy of MTP technology. Reducing the grade of feed refined methanol may be an effective method to save energy and reduce operation costs in MTP process. In this work, experiments and process simulation were carried out to investigate the influence and feasibility of degrading the methanol feed. Experiments were conducted to investigate the influence of crude methanol feed on conversion and selectivity of MTP reaction as well as the performance of ZSM-5 catalyst. The experimental results showed that degrading the methanol feed had no obvious influence on the conversion and selectivity of MTP reactions and the catalyst deactivation was caused by the carbon accumulation and metals deposition on the active sites. The process simulation results showed that the influence on the conversion and selectivity as well as the stream load of MTP process was negligible if 98 mol% methanol was used as feed. Finally, industrial experiments were conducted by adjusting the operation parameters to degrade of feed methanol of the commercial 500 kt·a^(-1) MTP unit of Ningmei Group in China. The results of industrial application illustrated that annually 180 kt fuel coal and 150 kt desalted water as well as 1770 MW·h^(-1) electricity would be saved when the water content increased from 0.01% to 0.4%. This work has identified the feasibility to improve MTP technology by degrading the methanol feed.